AgTalk Home
AgTalk Home
Search Forums | Classifieds (61) | Skins | Language
You are logged in as a guest. ( logon | register )

Swapping 25" tracks for 18" on our MT765D pics
View previous thread :: View next thread
   Forums List -> Machinery TalkMessage format
 
@farmerschneck
Posted 6/6/2015 13:07 (#4611789)
Subject: Swapping 25" tracks for 18" on our MT765D pics


Morrisburg, ON
Hi there, We made the jump to a tracked tractor this year. I read every thread on here about tracks before doing so and I'm glad I did. The only thing that the search function couldn't find was how to change tracks. So here it is. :D

I'm really pleased with the mt765d. It performed extremely well on our 24 row planter with the 25" belts. Next to no berming on the end rows and you could hardly see where it had been after the planter had made its marks. I'm now almost 100% certain that the threads on track berming being an issue are more about extremely jealous neighbours or really bad operators than the limitations of a 2 tracked tractor. After a day in the seat you figure out how to move your hand that little bit to make the perfect smooth turn. Yes if you turn too sharp too fast it will make a ridge. However if you do a brake stand (the wheeled equivalent to a poor tracked tractor operator) with a tractor with duals it makes a ditch too! From reading the search function threads I was very nervous about berming. On our clay-loam conventional tillage soils it isn't an issue at all. Sand I just don't know we farm next to none.

We are going to run the 25" camoplast 6500 belts for planting, land leveling and grain cart. The 18" camoplast 4500 belts will only be used to side dress corn.

This is the process of changing the tracks in photos. The missing parts and fine details are well outlined in the owners manual. The first belt took us 3.5 hours to completely change. The second one took just over an hour. I'm going to budget 3 hours total for the job in the future now that we know what we're doing and have made our mistakes. 2.5 people did the work over that time. 2 would work but that third set of eyes watching while mounting and dismounting was a big help.

Any questions or comments are welcome.

Warren

We purchased some heavy duty 20mt screw type jack stands that go from 28 to 48" high. We needed that height to support the tractor. I feel much safer with a stand in its lower half of operation than all the way up. The tractor was completely stable throughout the process.
 photo 20150526_120536.jpg

The tracks need to be about 8 inches off the ground to get the guide blocks to clear the drive wheel.
 photo 20150526_114439.jpg

The book instructions were pretty good. Very simple to take the pressure off the tracks using the provided hydrualic hose. A tip a farmer in Texas told me on twitter was to use the forklift to help get every last bit of oil out of the cylinder! Thanks Alan.
 photo 20150601_125105.jpg

I forget where I read this tip but it worked brilliantly. A light ratchet strap on the third bogey wheel keeps it from falling down when the tracks are loose.
 photo 20150601_125953.jpg

You have to loosen all the bolts on the bogies and the front idler wheel while the tracks are tight and the tractor is on the ground. They spin easily if you don't.
 photo 20150601_130504.jpg

I'm glad I listened to Nick Debuc (Soucey Engineer and college friend) and made the dealer let us keep the wide bogey wheels when we had them swap the wide drives for the mid sized. They really keep the 25 inch belt down and I think are helping with berming and wear.
 photo 20150601_130915.jpg

Next you remove the 3 outer bogies and the front outside idler wheel. Book says take the rear outer drive off but that's too much like work!
 photo 20150601_131126.jpg

We were unsure of the weight and opted to use the forklift for the first one. 2 people can easily carry the wheel so it wasn't necessary. Better safe than sorry!
 photo 20150601_131322.jpg

Ready to remove the track
 photo 20150601_131349.jpg

Our first setup at handling the track. Not recommended. See below for much more user friendly process.
 photo 20150601_133822.jpg

This worked slick! I suggest using straps to carry the belt instead of chains. The forklift holding the track wide over the drive wheel and the engine crane holding the front slack. The pallet jack didn't need to be pushed it just rolled along on its own. This setup saved us about half an hour verses the above photo.
 photo 20150601_143714.jpg

Swapped the bogey wheels and reattached the front idler. Then you can pressurize the track again.
 photo 20150601_144635.jpg

25 to 18 isn't a lot on paper but man it sure looks different!!!
 photo 20150601_153039.jpg

Side 2. Had it off in 30 minutes.
 photo 20150601_161658.jpg

Ready to re-align the front idler wheels to make the belt track properly.
 photo 20150601_172040.jpg
Top of the page Bottom of the page


Jump to forum :
Search this forum
Printer friendly version
E-mail a link to this thread

(Delete cookies)